Hi All,
I’ve renewed the N75 (oem), N249 and diverter valve. Thoroughly checked all hoses and clamps visually (but not smoke/leak tested).
I’ve put a bicycle pump on the waste-gate actuator line and verified that it opens somewhere around 5 - 10 psi (hard to tell exact pressure as the gauge is not of a suitable scale). I can move the waste-gate linkage very easily by hand but I’ve read that it should be a bit harder(?).
In first and second I’m now getting boost peaks around 35 psi (and often blowing the hose off TC outlet).
On a long push in 3rd, boost settles nicely at 15 psi. On two occasions near the top of the rev range, say 5000 to 5500 rpm, car seemed to go in to safe/limp mode and boost dropped to 5-6 psi.
I’m thinking wastegate actuator might be too slow to regulate boost in the short term (e.g. 1st and 2nd). Possible leaky diaphragm on the actuator.
Also, possibly ECU needs reset by battery disconnection.
Anyone have any diagnosis that fits these symptoms? Any ideas for further tests and checks to identify the problem?
I’m using an Bluetooth OBDlink MX+ and it’s app to get and log data. It only updates once a second and doesn’t get all the data I need (e.g. boost demand). Anyone know of software I can use with this and iPad to get more data channels and better frequency of data?