Some time has gone by and a few issues have come up and they just HAD to be annoying to solve.
It had a weird mis/cut when boosting which was the worst thing in the world and it would get worse in higher gears and it took a while to solve... Thought it might've been alternator letting go or some weird Knock limit cutting -5° timing out of the table. But it turns out it was Boost cut kicking in, tuner sent a fix table but it hits about 17-15psi according to the gauge, so I've been doing some adjustment to the wastegate trim to see if I can make it stay around 20psi (which it's meant to be at).
There was a few issues with boost... Solved (hopefully) after water pump, but there was 1 point where it would keep blowing off:
Really annoying but we fixed it with some cut, bend & weld.
So far its been kinda working with cut still kicking sometimes but after the drive I realized I was trying to set it around 250-260kpa which is about 22psi boost (cut is 265kpa) instead of ~240kpa which thankfully I think I've solved. So now it should hit 20psi in all gears and not get stuck sitting under 20psi when trying to go in 3rd or 4th.
But thats been the current challenge, the one just before this was much harder, annoying and painful. Water pump leak was fixed after 3 pumps combined into 1. Initial pump we got was the fixed tension 2.2L one which at first leaked because the O-ring was the wrong size, then we got the proper one with slides (7A & NG had water pump do the tension for the timing belt which is pretty smart). Went on fairly well, only trouble was the blades being longer than the others so it was a struggle but it worked nonetheless. Until I tried to get the belt on and figured out the gear/cog was wrong and didn't mesh with the belt (different tooth gaps) which was even more annoying...
So then I tried the fixed tension one again but with the good O-ring from the adjustable pump, which then got 80% of the way until I turned the car on & it started whining extremely loud.. Fixed tension doesn't work with this setup
So in a last ditch effort before going insane was: Swap the gear from the fixed tension one into the adjustable tension housing... Surprisingly enough, after some screwing around on a press it had actually worked.
Went on, no leaks, no whining, literally perfect. Instead of the 2-3h it should've taken, it took 3-4 days & lots of cuts on my hands (one of which cut a few mm in my thumb)
Aside from the most annoying water pump ever seen, and me actually taking a plunge into learning how to tune the car is going fairly well. I think it has some torque steer when boost hits but that could be the "Unpowered-power steering" doing some wandering but eh.
The car sounds insane, it looks really unassuming, but it goes like nothing I've ever been in before.
Next on the list... Redo coil wiring, up the alternator to +120A, actual fuel tank. Criteria for next time it gets tuned after these things is: Higher Revs (7.5k lim), More Boost, Less Timing Advance (I'm staying with 98 Octane).